JUNE 2019
 
June 18, 2019:  4.17BO 0.41 water  Low on water.  we need to replace several silicone grommets in the radiator to stop leaks.  This is not an expensive repair. 
June 17, 2019:  5.01 BO - 0.41 water
June 16, 2019:  5.01 BO - 0.75 water
June 15, 2019:  5.01 BO - 1.67 water
June 14, 2019:  5.84 BO - 0 water
June 13, 2019:  5.63 BO - 1.25 water
June 12, 209:  6.68 BO & 0.83 water
June 11, 2019: 4.17 BO & 2.5 water
June 10, 2019:  5.01 BO & 1.67 water
June 9, 2019:  5.01 BO & 2.5 water
June 8, 2019:  5.01 BO & 1.67 water.  We are getting back a gritty fluid.  We had not retrieved all the fluids from our recent treatment and we believe this is part of that operation
June 7, 2019:  5.85 oil & 1.67 water
June 6, 2018:  In 22 hours the well produced 10.02 BO and 1.67 water
June 5, 2019:  Wellhead arrived and installed by noon. 
MAY 2019
 
May 29, 2019:  We have been waiting for the part to arrive to repair the motor on the pumpjack.  Today we learned recent violent weather in Oklahoma is the reason for the delay.  A tornado touched down about 1/2 mile from the plant and it knocked out all power to the area.  In addition flooding from the storms have restricted access to the facility.  They are hopeful they will be able to return to the plant by the end of the week and should be able to ship out our part early next week. 
May 13, 2019:  When we were able to return to the Byrd we found the B2H was not pumping.  The issue was diagnosed as a cracked head.  
May 10, 2019:  Due to the recent rains, we remain unable to reach the lease due to road conditions
May 5, 2019:  Unable to reach the lease due to rains.
May 4, 2019:  5.01Bo - 1.67 water.  Reporting 20 hours
May 3, 2019:  5.85 BO - 0.83 water
May 2, 2019:  5.01 BO - 1.67 water
May 1, 2019:  4.18 BO - 0.83 water

APRIL 2019

April 30, 2019:  5.80 BO - 0.83 water
April 29, 2019:  5.01 BO - 0 water
April 28, 2019: 5.01BO - 0 water.  The unit was down due to low water level.  added water and started back up.
April 27, 2019:  6.68 BO - 0.83 water  23 hours
April 26, 2019:  3.34 BO - 2.50 water,  Unit was down and fire out on the heater.  It started up on casing gas and we are monitoring.  It began pumping solid water again which may indicate another source is trying to feed in...which would be excellent news
April 25, 2019:  5.85 BO - 0 Water
April 24, 2019:  5.84 BO - 1.67 water
April 23, 2019:  6.68 BO - 0.83 water
April 22, 2019:  5.85 BO - 0.5 water
April 21, 2019:  6.68 BO - 1.67 water...23 hours
April 20, 2019:  8.35 BO - 4.17 water...it appears it is beginning to work
April 19, 2019:  6.68 BO - 2.5 water...23 hours reported
April 18, 2019:  8.35 BO - 1.67 water
April 17, 2019:  4.17 BO - 4.17 water.  The unit went down in overnight storms
April 16, 2019:4.17 BO - 6.68 water.  Still pulling nasty water...which is good...we are cleaning out the trash Moran Lavaca dumped down the well
April 15, 2019:  2.5 BO - 19.2 water.  It appears we are cutting a new channel which should lead to nice production once we clean out the well.
April 14, 2019:  2.05 BO - 18.37 water
April 13, 2019:  0 BO - 7.51 water - very dirty but does appear the chemical is working and is cleaning out the well
April 12, 2019: 0.42 BO - 5.84 water 
April 11, 2019:  0.42 BO - 5.84 water
April 10, 2019:  0.85 BO - 5.84 water
April 09, 2019:  0.83 BO and 6.68 BW
April 08, 2019:  3 BW - Able to switch from propane over to casing gas 
April 07, 2019:  Removed 33.4 bbl water
April 06, 2019:  Removed 30.06 bbl water in 20 hours
April 05, 2019:  Removed 35.07 bbl soapy water 
April 04, 2019:  7BO and 12bbl water.  The unit was down as it lost gas.  Will purchase propane to run jack. 
April 03, 2019:  7BO 12 BW
The unit went down when we lost gas at the heater.  We are buying a load of propane to run the jack until the well can again make enough gas.  
April 02, 2019:  Unit began running.  The casing has very little pressure and there is low BTU.
April 01, 019:  Casing has little pressure so we chose not to try to run the motor.  Waiting for the pressure to build and we can run the jack off our produced gas. 

MARCH 2019

March 28, 2019:  Well was stimulated early this morning.  Will remain shut in until Saturday morning, March 30.  

March 27, 2019:  Well shut in for treatment

March 26, 2019:  Well shut in for service

March 25, 2019:  Sold approximately 168.63 BO

March 24, 2019: Called dispatch to take a load

March 23, 2019:  3.35 BO - 0 water

March 22, 2019:  3.34 BO - 0 Water

March 21, 2019:  3.35BO - 0 water 

March 20, 2019:  2.05 BO - 0 water....the plan is to produce enough for a load in March and then conduct a soap stimulation.  Otherwise, we will not have enough production for a load in April. 

March 19, 2019:  3.35 BO - 1.67 water  We need 3 more days of a minimum of 3 barrels to have a load.  We may also need to consider a soap treatment to clean out the well. 

March 18, 2019:  3.34 BO - 1.67 water

March 17, 2019:  1.67 BO - 0.835 water

March 16, 2019:  Will need to replace the valve   

March 15, 2019: Again attempted the repair

March 14, 2019:  Attempted repair.  

March 13, 2019:  Split tubing...casing tube was oil wet behind the check valve.  Oil is just circulating and not going to tank.  

March 12, 2019:  4.6 BO 0.84 water

March 11, 2019:  5.01 BO, 2.74 eater

March 10, 2019:  3.34 BO, 0 water

March 09, 2019: 4.17 BO, 0 water

March 08, 2019:  5.01BO, 0 water

March 07, 2019:  3.34 BO, 0 water

March 06, 2019:  5.01 BO no water

March 05, 2019:  3.34 BO no water

March 04, 2019:  5.84 BO no water

March 03, 2019:  3.34 BO no water

March 02, 2019:  1.67 BO with 1.67 water

March 01, 2019:  4.17 BO no water

 

FEBRUARY 2019

 

February 28, 2019:   205 BO and 1.67 water  We are exploring the idea of putting it back on the eater with 20psi.  We are checking gas production to see if it has increased as oil has not. 

February 27, 2019:  4.17 BO no water.  Gas blowing on tubing has increased from the day before

February 26, 2019:   3.34 BO  Everything is operating as it should. 

February 25, 2019:  6.68 BO in 17.5 hours

February 24, 2019:  0.835 BO  Unit was down.  Heater had 3psi.  The tubing was basically dead.  Restarted unit.

February 23, 2019:  8.35 bbls fluid...nice increase

February 22, 2019:  5.01 bbls of fluids.  The wind accidentally knocked test kit into the tank.  It will be Monday before it can be replaced, and we will be able to distinguish oil levels for water.

 

February 21, 2019:  3.34 oil with 3.34 water

Set tubing pressure to 30psi and holding casing pressure at 9psi.  Moved quite a bit of solids with water slug.

February 20, 2019:  ENCOURAGING NEWS.  In 19 hours the B2H produced 3.34 BO and 8.35 water.  By lowering the pressure it appears it is beginning to come to us.  The brine water is heavy so if it can bring up that volume of brine water it can bring up oil.  Getting rid of water is a good thing.  I will be most interested in seeing what it does for the next few days!  

February 20, 2019:  we separated the casing and tubing about 1 PM.  Tubing is going straight to the tank and we set casing pressure at 9psi.  We now wait to see if the B2H likes this combination. 

February 19, 2019:  3.34 BO no water

February 18, 2019:  3.757 BO no water

February 17, 2019:  4.175  BO no water  80psi

February 16, 2019:  4.175 BO no water

February 15, 2019:  6.68 BO - no water.  Hauled a load today. 

February 14, 2019:  3.34 Bo with 0.4175 water.  We are reducing the tubing pressure to 80psi

February 13, 2019:  Success, we are back in business...5.845 BO - no water

February 12, 2019:  No production.  The well was pressured up at 130psi.  Everything is operating.  Decided to back off the pressure 50# and see what happens. 

February 11, 2019:  4.18 BO no water.  The tubing pressure has stabilized at 130PSI.

February 10, 2019: We lost fluid in the tubing when it went down due to the spark plug issue

February 9, 2018:  5.84 BO with no water - 21 hours since last checking the well 

February 8, 2019:  The ignition system was replaced 

February 5, 2019: 5.01 BO with 0.83 water

February 4, 2019:  0.41 BO - no water, just pumped from being down

February 3, 2019:  1.67 BO - no water, jack down as the spark plug needed

to be replaced

February 2, 2019:  6.67BO - no water

February 1, 2019:  6.67BO - no water

 

 

 

JANUARY 2019

 

January 31, 2019:  5.01 BO - no water

January 30, 2019:  Loaded up with trash

January 29, 2019:  6.68 BO - no water

January 28, 2019:  6.68 BO - no water

January 27, 2019:  5.84 BO - no water

January 26, 2019:  4.6 NO - no water.  Our gauger made his round 7.5 hours earlier than usual which would impact the production reported today. 

January 25, 2019:  6.68 BO - no water

January 24, 2019:  5.01BO no water

January 23, 2019:  0.8357BO - no water   We had trash in the tubing regulator that needed to be cleaned out.

January 22, 2019:  5.84BO - 0.835 water

January 21, 2019:  6.68BO - no water

January 20, 2019:  6.68BO - no water

January 19, 2019:  6.68BO - no water

January 18, 2019:  6.68 BO - 3.34 water  We sold a load of approximately 177.39 BO.  Our negotiations with CML have gone well and they appear eager to assist us.  The remaining issue appears to be their sour gas and we will need to have the approval of Enterprise Midstream to move forward.  I am hopeful that will happen this coming week. 

January 17, 2019:  6.68 Bo - no water

January 16, 2019:  5.01 BO - 1.67 water.  We reset the weights on the pumpjack so it will run more efficiently and we will experience less wear and tear on our equipment.

January 15, 2019:  4.14 BO with 3.34 barrels water  We should have the load ready to go by tomorrow. 

January 14, 2019:  5.84 BO 0.5 water  Anticipate we will have a load ready to go out by Friday.

January 13, 2019:  4.17 BO 3.34 water

January 12, 2019:  5.84 BO no water (He came early which could explain for the lower production).  Our pumper (his name is Scott...but not Payn) is finishing a project on another lease  & when completed will run our product through the heater to get it ready to sell.  I anticipate we will be ready to sell a load about the 20th of January.

January 11, 2019:  6.68 BO no water

January 10, 2019:  6.68BO no wanter

January 9, 2019:  7.51 BO no water

January 8, 2019:  6.68 BO with no water

January 7, 2019:  4.27 BO with 2.5 BW

January 6, 2019:  Back in business...10.02BO with no water. 

January 5, 2019:  5.84 BO with no water.  The tubing regulator was trashed up and we lost back pressure.  It was cleaned out and we increased the psi from 75 to 95#.  This may help to keep the trash from building up. 

January 4, 2019:  10.02 BO with 1067 water

January 3, 2019:  5.01BO and 0.83 water

January 2, 2019:  HAPPY NEW YEAR!  We did get out a December load of 162.48 BO (unofficial).  In the past 24-hours, the B2H has produced 8.35BO with no water.  Oil prices have been climbing all day today... a nice way to kick off the New Year. 

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